Descargar Imprimir esta página

Cebora 387 Manual De Instrucciones página 18

Ocultar thumbs Ver también para 387:

Publicidad

Idiomas disponibles

Idiomas disponibles

CEBORA S.p.A.
6.2
Error Code Table.
Listed below the "Error Code Table". For a detailed description of the displayed service codes please
refer to the "Service Manual" of the Power Source.
Error
code
2
EEPROM error.
CAN bus communication error between
Wire Feeder and Power Source, or
6
between Control Panel and Power Source
(detected by Power Source).
CAN bus communication error between
"rob int"
Robot and Control board (detected by
7
Control board).
CAN bus error: Control Panel doesn't
GB
9
communicate
(detected by Control Panel).
Output voltage and output current null,
10
with start button pressed. Voltage or
current detecting circuits damaged.
At start up, no communication with
13
Precharge board.
Microprocessor supply voltage error, on
14
Micro board.
15
Precharge board output DC voltage lower
(only 389)
than preview value.
Precharge board output DC voltage lower
16
than allowed minimum value (400 Vdc).
Voltage
17
capacitor higher than voltage across
(only 389)
positive connected capacitor.
Voltage
18
capacitor lower than voltage across
(only 389)
positive connected capacitor.
19
During working, no communication with
(only 389)
Precharge board.
Master
20
missing.
25
EPLD Fault. Primary current excessive.
30
Incorrect trimmer set on master module.
41
Connector/Robot board disconnected.
Encoder
42
between set point and measured speed).
Connector board communication error
43
(serial UART).
3300305-B
Error description
with
Control
board
across
negative
connected
across
negative
connected
"interlock"
module
signal
error
(excessive
difference
Solutions
Replace Control board.
Alarm detected by Control board. Check CAN bus
connection between Control board, Motor Control board
and Panel Control. Make sure compatibility of the
program releases inserted into the boards. Replace
Control, and/or Control Panel and/or Motor Control
boards.
Alarm detected by Control board. Check CAN bus
connection between Control board, Motor Control board
and Robot. Make sure compatibility of the program
releases inserted into the boards. Replace Control and/or
Motor Control boards.
Alarm detected by Control Panel. Check CAN bus
connection between Control Panel and Control board.
Make sure compatibility of the program releases inserted
into the boards. Replace Control and/or Control Panel.
Replace Control and/or Driver and/or Igbt boards. Replace
Power Transformer and/or Diode Group and/or output
Inductor and/or current Transducer.
Check wiring between Precharge and Control boards.
Replace Precharge and/or Control boards.
Check wiring between Micro and Flyback boards. Replace
Control and/or Flyback boards.
Check mains voltage conditions. Make sure Rectifier
Bridge, DC-capacitors or Igbt Group are not in short
circuit. Replace Precharge and/or Control boards.
Check mains voltage conditions. Make sure Rectifier
Bridge, DC-capacitors or Igbt Group are not in short
circuit. Replace Precharge and/or Control boards.
Check wiring between Precharge board and DC-
capacitors. Replace DC-capacitors and/or discharge
Resistors and/or Precharge board.
Check wiring between Precharge board and DC-
capacitors. Replace DC-capacitors and/or discharge
Resistors and/or Precharge board.
Check wiring between Precharge and Control boards.
Replace Precharge and/or Control boards.
Check terminals 3 and 4 of J1 on TA board are connected
between them. Replace TA and/or Control boards.
Replace Control and/or Driver and/or TA boards. Replace
inverter Igbt and/or Power Transformer and/or secondary
Diode Group.
Perform trimmer adjusting procedure on Control board,
following Power Source Service Manual instructions.
Replace Control board.
Replace Motor Control and/or Connector boards.
Replace Encoder or Wire Feeder Motor and/or Motor
Control board.
Check flat-cable between Connector and Motor Control
boards. Replace Connector and/or Motor Control boards.
18
18-03-2016

Publicidad

loading

Este manual también es adecuado para:

389